June Jamboree at Laguna Seca - 06/27-29/03

Qualify

Race

Chart

Race2

Chart2

http://www.sfrscca.org/Results/20030629/

Hello all,

 

Well we've had our first race after the TPS (throttle positioning sensor, the doohickey that tells the computer where your foot is) was "really" fixed/replaced. So your wondering "Did it make a difference?", well I think it did but I'll let the times tell the story.

 

Practice I ran a 1:51.8, qualifying I ran a 1:51.4, and during the race on Saturday I ran a 1:51.288 running second almost the entire race. On Saturday qualifying I ran a 0.00.0 (read on to find out why). For Sunday's race I ran a 1:50.735 the second fastest ITA car on the track! So I guess the car is back to where we started at the beginning of the year. In fact Steve Borlik, who finished first and is first in points, commented that I scared him by running so close with him on Saturday. :-)

 

Now your' wondering what happened to get me a 0:00.0 or really a no qualify. Well what happened was that I was running around the track in a comfortable second place not really able to challenge for first since that restart in fourth gear where I should have been in third really put a gap between Steve and I. I also had to pass the ITS cars that passed me on that restart making first even more elusive. Oh yeah back to what happened. Well like I was saying I was running a long comfortably in second place when all of a sudden, okay not really all of a sudden but within a couple of turns, the lower ball joint (lbj) and the front knuckle decided to separate. Now I didn't give anybody permission to do this so I promptly parked the car off of the track and gave the ball joint a real talking to. Well maybe it happened like that or maybe not the result was the same. Five minutes before the end of the race I found myself with a car in last place.

 

The car was towed back to impound. We pulled the wheel off and discovered that the castle nut was gone. Some how the cotter pin that is supposed to prevent this was gone and the castley nut had worked it's way free. As it turned out, what looked to be an easy thing to fix wasn't. The threaded part of the lbj was bent preventing us from just replacing the castle nut. We took that car back to our paddock spot to replace the lbj. As we struggled to press the lbj out of the lower control arm (lca), with out success, I discovered that this was my backup lca that had the lbj welded in place. We had to take the lca off of the car and take it to a welder. Luckily there was one at the track. Unluckily someone had assembled the lca off of the car and now that the subframe was on the car I found that someone had put in one of the bolts the wrong way. We had to cut the bolt off in order to get the lca off. The above process needless to say took some time and we were not able to make qualifying. At this time we still hadn't taken the part to the welder.

 

I did finally get the part to the welder who said he could have it done by 7:30 or so. So the only thing left to do was to hang out with the crew and my sponsors, Joey and David of D&J Racing. They had been very generous this weekend bringing up a case of 20w50 RedLine Racing Oil and offering to pickup the cost of the welding. We checked on the welder around 8ish and he still was working on other stuff. So we went back to sit around some more. Around 9 I suggest everybody head home and I'd camp out to wait for the welder to finish. I checked back every hour or so and by 1:30AM on Sunday I decided to turn in.

 

Later that Sunday morning I checked with him. He was just finishing up and by 8AM I had the part back and started installing it. Things went together well and we took the car over to tech before 10AM. We passed tech. Now the only things left to do was to top off the tank and to align the car. We were all done and ready to go by 11AM. The rest is history. ;->